Scary/Smokie oil leak at Boost!
#42
WoW!
Just trying to buy a bit of time (I hope).......
I've got properly drained oil line & correctly routed pvc. Haven't had a problem till now....somethings changed? (for the worse) I'll be doing a leak down test shortly, hope this will pinpoint the problem. I'm not sure if I'd want to spend a lot of money on parts on this engine when you can sometimes source a used engine for lil' money.
Peace
Mike
http://www.cardomain.com/ride/179116
Just trying to buy a bit of time (I hope).......
I've got properly drained oil line & correctly routed pvc. Haven't had a problem till now....somethings changed? (for the worse) I'll be doing a leak down test shortly, hope this will pinpoint the problem. I'm not sure if I'd want to spend a lot of money on parts on this engine when you can sometimes source a used engine for lil' money.
Peace
Mike
http://www.cardomain.com/ride/179116
#44
While the PCV routing pre-turbo may be correct, it isn't the solution to this problem. The only thing being accomplished by the pre-turbo routing would be to dump a pile of oil into the intake. Wonder how the turbo would enjoy sucking in fluid at the rate it sounds like this guy is losing it?
#46
You are right, I don't know for sure. However ....
The amount of oil described here would indicate a pretty serious problem.
And I assume he has now routed it correctly and still having the problem.
I would conclude it is something other than the PCV routing.
I checked it out today, and he has a diaper around his filter on the cam cover. It's alot of oil
correctly routed pvc
I would conclude it is something other than the PCV routing.
#47
UPDATE:
Well, got a day off to take the head off. Before I did that, compression test showed 120/92/95/150. Head came off the block with no problem once the bolts were out it just slid off? Expected it to be stuck somewhat? Gasket looked to be in good shape, valves looked good?
Well, here's the bad part, the back piston (firewall) edge had eroded (melted).
Also found oil in the intake side of the turbo, now i'm wondering if the oil seal let go on that as well?
Mike
Well, got a day off to take the head off. Before I did that, compression test showed 120/92/95/150. Head came off the block with no problem once the bolts were out it just slid off? Expected it to be stuck somewhat? Gasket looked to be in good shape, valves looked good?
Well, here's the bad part, the back piston (firewall) edge had eroded (melted).
Also found oil in the intake side of the turbo, now i'm wondering if the oil seal let go on that as well?
Mike
#48
Boost Czar
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no, because your were letting compression past the rings, and that positve pressure was blowing oil into intake VIA the breather port.
examine the intake more closely you'll see that was the source of the oil, not the turbo.
examine the intake more closely you'll see that was the source of the oil, not the turbo.
#52
For the life of me I couldn't understand how oil could have gotten in the intake, as I mentioned I didn't have a vent tube routed into the intake. HST, I never thought about the case pressure blowing back into the oil return line? That would make sense?
TIA
Mike
TIA
Mike
Last edited by mracer; 06-03-2007 at 10:49 PM. Reason: Doh!
#55
lol... what u gotta do is... weld a bung or something onto your exhuast and then run a line to that bung off the head filter where u hada your filter on... that was it creates vaccumm from the exhaust ...and oil that gets blown by just gets burnt off in your exhaust instead of lowering the octane of your gas and creating harmful knock...
just kidding...but damn i would do it. lol lol
just kidding...but damn i would do it. lol lol
#59
OKay, quick update.....
Got the pistons out, of course, for all the well known reason of making our engine RWD, #4 piston looked the worse. All 4 pistons have broken top lands. #4 bore had some slight scuffing, the other 3 looked pristeen. Brgs. looked good. Gonna look into getting some low compression Wiseco's.
Mike
Got the pistons out, of course, for all the well known reason of making our engine RWD, #4 piston looked the worse. All 4 pistons have broken top lands. #4 bore had some slight scuffing, the other 3 looked pristeen. Brgs. looked good. Gonna look into getting some low compression Wiseco's.
Mike