Car makes noticably less power after Autobahn incident (intercooler pipe came loose)
#1
Car makes noticably less power after Autobahn incident (intercooler pipe came loose)
First things first. About a month ago I was cruising on the Autobahn. 5 miles into Germany I did some pulls close to 150mph to check the top speed. (which went bloody hell great btw.) I decided it was enough and cruised a bit at 125mph for another 2 miles or so. Wanted to overtake a car, went in boost a bit and.... WOOSH, PPUPHHHH... no performance... pulled the car over to the side and stopped, car died because it couldn't keep an idle. (In total I was still less than 10 miles into Germany so the fun was short.)
After the first moment of 'omg what just happened? did I blow my engine?!' I realised the engine and internals weren't blown and it was probably something else. Stupid thing was I couldn't find a pipe/hose loose at the turbo/intercooler or anything, neither did the German ADAC guy with the enormous beer-belly.
After waiting for more than two hours we finally got on top of a flatbed towtruck and drove to the nearest Mazda dealership. (ADAC thought they would know the car.) Well of course they didn't understand a lot because of all the mods, but luckily I finally spotted the problem. (why I did spot it this time I do not know) The pipe that goes into the air outlet at the turbo was completely loose. (I could stick my finger between the gap) With my current but old FM II kit this is a metal pipe.
So I fixed that easily and the car started just fine. AFR also fine, etc. I went home and staid in vacuum all the way, still quite scared and I didn't want to stress the car before I talked to some people with more skills and know-how.
Together with a good friend of mine (and driver of a 300+ whp miata) we fully checked the car. I noticed that it had less performance and that the old Bosch BPV sounded different. We took every pipe and hose apart and installed everything properly again. Also installed a 'new' BPV (the bigger, old FM unit) The thing is, the car drives great. revs happily, starts easily, nothing to worry about, solid AFR's, etc. BUT like with the old BPV after the incident, performance is noticeably worse.
It looks like I'm making at least a psi or so less boost, but more noticeably it feels like I'm spooling up A LOT later and slower. Feels like I'm missing 30 horses if it ain't more. The wastegate actuator was a bit loose but after fixing that still no difference. I'm also hearing a very faint high pitched 'shhhhh' sound when accelerating. Only audible at speeds less than 20mph though. I guess it's probably a slight vacuum leak? (But man, that could never cause this, right? Idle is fine...)
Any ideas what to check/do?
Thanks guys!
PS
I'm running a 1998 NB, Old FM II turbo kit so with the Link piggyback ECU and 4 extra injectors placed in the intake manifold. FM 2.5" exhaust system, happy meal clutch/flywheel kit.
NGK sparkplugs, 8.5mm leads, new oils all around, new K&N filter.
Car dyno tuned last year or so, 246hp on the engine, 300nm (220ft lb)
After the first moment of 'omg what just happened? did I blow my engine?!' I realised the engine and internals weren't blown and it was probably something else. Stupid thing was I couldn't find a pipe/hose loose at the turbo/intercooler or anything, neither did the German ADAC guy with the enormous beer-belly.
After waiting for more than two hours we finally got on top of a flatbed towtruck and drove to the nearest Mazda dealership. (ADAC thought they would know the car.) Well of course they didn't understand a lot because of all the mods, but luckily I finally spotted the problem. (why I did spot it this time I do not know) The pipe that goes into the air outlet at the turbo was completely loose. (I could stick my finger between the gap) With my current but old FM II kit this is a metal pipe.
So I fixed that easily and the car started just fine. AFR also fine, etc. I went home and staid in vacuum all the way, still quite scared and I didn't want to stress the car before I talked to some people with more skills and know-how.
Together with a good friend of mine (and driver of a 300+ whp miata) we fully checked the car. I noticed that it had less performance and that the old Bosch BPV sounded different. We took every pipe and hose apart and installed everything properly again. Also installed a 'new' BPV (the bigger, old FM unit) The thing is, the car drives great. revs happily, starts easily, nothing to worry about, solid AFR's, etc. BUT like with the old BPV after the incident, performance is noticeably worse.
It looks like I'm making at least a psi or so less boost, but more noticeably it feels like I'm spooling up A LOT later and slower. Feels like I'm missing 30 horses if it ain't more. The wastegate actuator was a bit loose but after fixing that still no difference. I'm also hearing a very faint high pitched 'shhhhh' sound when accelerating. Only audible at speeds less than 20mph though. I guess it's probably a slight vacuum leak? (But man, that could never cause this, right? Idle is fine...)
Any ideas what to check/do?
Thanks guys!
PS
I'm running a 1998 NB, Old FM II turbo kit so with the Link piggyback ECU and 4 extra injectors placed in the intake manifold. FM 2.5" exhaust system, happy meal clutch/flywheel kit.
NGK sparkplugs, 8.5mm leads, new oils all around, new K&N filter.
Car dyno tuned last year or so, 246hp on the engine, 300nm (220ft lb)
Last edited by prxprx; 09-23-2012 at 12:56 PM.
#3
Ah, yeah some more details would probably be smart...
1998 NB, Old FM II turbo kit so with the Link piggyback ECU and 4 extra injectors placed in the intake manifold. FM 2.5" exhaust system, happy meal clutch/flywheel kit.
NGK sparkplugs, 8.5mm leads, new oils all around, new K&N filter.
Car dyno tuned last year or so, 246hp on the engine, 300nm (220ft lb)
(slightly old picture)
1998 NB, Old FM II turbo kit so with the Link piggyback ECU and 4 extra injectors placed in the intake manifold. FM 2.5" exhaust system, happy meal clutch/flywheel kit.
NGK sparkplugs, 8.5mm leads, new oils all around, new K&N filter.
Car dyno tuned last year or so, 246hp on the engine, 300nm (220ft lb)
(slightly old picture)
#7
Nope I immediately lifted throttle and did not try to do anything other than rolling to a stop on the side of the autobahn. It stalled immediately which isn't extremely good for the turbo and stuff, but I don't think it can cause my symptoms.
I'm not a tech kinda guy so at first I didn't knew what just happened so I was extremely careful, lol.
It's strange because the car drives absolutely fine... Darn it, I might just need to do a dyno to see if it's not all in my head.
I'm not a tech kinda guy so at first I didn't knew what just happened so I was extremely careful, lol.
It's strange because the car drives absolutely fine... Darn it, I might just need to do a dyno to see if it's not all in my head.
#10
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Did you hook up a boost leak tester and try that? You could just have a leak somewhere. Or what are you using for a boost controller? Could you have hit it while you were re-installing everything, and it just needs to be re-adjusted back to your target boost?
#11
Not tests yet, I'll try to find a boost leak tester locally or I'll try to make one myself.
About the boost controller, ouch... I actually can't remember exactly what I have, it's on the tip of my tongue... Anyway, cou can see it here, to the right next to the air filter: http://img.photobucket.com/albums/v4...ject/groot.jpg
We definitely haven't hit that.
About the boost controller, ouch... I actually can't remember exactly what I have, it's on the tip of my tongue... Anyway, cou can see it here, to the right next to the air filter: http://img.photobucket.com/albums/v4...ject/groot.jpg
We definitely haven't hit that.
#13
The turbo spins freely by hand, yes? Do you have a CAT in your exhaust? A ~150mph pull at your (previous) power level produces a LOT of heat for a lot of time. Unless you have some special aero work, that last 10mph takes quite a while. Make sure your troubleshooting include things that might have melted in addition to what might have popped loose.
#14
Check out every single coupler, take it apart, clean the surfaces to ensure theres no oil and tighten it up again. Also disconnect the blow off valve from the intake manifold and plug the hole and do a run. Yes you'll get surge in the process but see if hear the high pitched noise again.
The turbo spins freely by hand, yes? Do you have a CAT in your exhaust? A ~150mph pull at your (previous) power level produces a LOT of heat for a lot of time. Unless you have some special aero work, that last 10mph takes quite a while. Make sure your troubleshooting include things that might have melted in addition to what might have popped loose.
#15
I have two friends with FMII cars that mysteriously lost power. Both causes: Disintegrated CATS. These cars live 3,500 miles apart, the owners don't know each other and the CATS were purchased and failed over a year apart. I saw one of the slags in person. It blew to pieces and melted in place - one giant lump of crap that had a fast car putting down ~155whp on the dyno.
If you don't find any of the simple things discussed already, I would pull the down pipe and take a peek. If it looks like the one I saw, bang it out of there and see if you can hit 160 on the way out of town!
If you don't find any of the simple things discussed already, I would pull the down pipe and take a peek. If it looks like the one I saw, bang it out of there and see if you can hit 160 on the way out of town!
#16
I have two friends with FMII cars that mysteriously lost power. Both causes: Disintegrated CATS. These cars live 3,500 miles apart, the owners don't know each other and the CATS were purchased and failed over a year apart. I saw one of the slags in person. It blew to pieces and melted in place - one giant lump of crap that had a fast car putting down ~155whp on the dyno.
If you don't find any of the simple things discussed already, I would pull the down pipe and take a peek. If it looks like the one I saw, bang it out of there and see if you can hit 160 on the way out of town!
If you don't find any of the simple things discussed already, I would pull the down pipe and take a peek. If it looks like the one I saw, bang it out of there and see if you can hit 160 on the way out of town!
#17
Hopefully not but talking to two different 'miata' buddies in the last month (one local and I saw it with my own eyes), both had failed FM cats that produced symptoms just like you are describing. If it turns out to be the problem, you're best best is to find a performance shop there and have them weld a new equivalent one in. Hopefully there are no bogus BS rules about non-OEM parts and other such crap. Good luck with everything!