I should mention with the proper gasket you shouldn't NEED RTV, especially with something like the throttle body. I mean, heaven forbid you get a new gasket :giggle: Not like its coming off now though :rofl:
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Originally Posted by RotorNutFD3S
(Post 1121571)
FWIW, the $20 oil pressure test kit from Harbor Freight works great. Just went through something similar (and a slight panic) when my aftermarket gauge sender took a crap.
Originally Posted by EO2K
(Post 1121600)
I should mention with the proper gasket you shouldn't NEED RTV, especially with something like the throttle body. I mean, heaven forbid you get a new gasket :giggle: Not like its coming off now though :rofl:
They essentially do the same thing ;) This way, if the bolts fall out, I know it isn't going anywhere! I'm at the point where I will do anything to spend no more money on the car. I'd rather start putting the money towards a down payment on a house. |
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OK a little progress tonight. I bought a shitty napa mechanical gauge to do an independent test of the oil system. Yanked the sensor off the block and installed it.
First I decided to try to bleed some of the air out of the lines. I ripped some clear tubing off my brake bleeder and taped it to the vacuum as well as I could. Then I jammed it in the hole as well as I could and bled until the majority of the air came out. I did this on the sensor bung and the turbo oil feed line. https://www.miataturbo.net/attachmen...ine=1397535470 Then I hooked up the gauge and cranked for around 10-15 seconds. I saw around 30 psi on the gauge, but I never trust the shitty hard line compression brass fittings on these things(mostly talking about plumbing experiences). Soooo making progress at least! I'm hoping that it is just a minor leak in the hard line and having not started the motor to really get some pressure in the line. Is it normal, when you stop cranking the motor, for pressure to bleed off immediately? Just trying to think what else I can try here. Maybe replace the hard line with clear tubing? and use a hose clamp to clamp it down? So 30 psi is a low reading of what the motor is actually developing I hope. I will say I saw a much quicker response pressure wise after vacuuming the air out of the lines. Shitty gauge picture. I tried to find a oil pressure bleeder, but I don't have a harbour freight close by. https://www.miataturbo.net/attachmen...ine=1397535470 |
Pressure stops immediately because liquids don't compress and the oil has a place to go. Glad you saw pressure.
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30psi is really good for just the starter. Plug everything back in a start the motor. You're fine.
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+1 - fire her up...!
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Awesome, thanks guys, I thought it needed to develop +/- 60 PSI.
Wired in my flyback correctly on my Idle Valve wires a la: https://www.miataturbo.net/attachmen...ine=1397562026 Tested continuity on the EBC, which didn't respond. Stripped back the shrink wrap and found the flyback diode had broken probably due to me tugging on the wiring to route it. So a new diode and we are back in business. I put a couple extra layers of shrink wrap around the soldered area to strengthen it up. I reinstalled the OEM oil sensor and connected the gauge back up. Right now I'm trying to figure out why I still can't get the tach to work. As per Zaphod's completely over the top wiring diagram he made for me, the tach out signal on the DB12 connector, 2B, is being routed to the yellow/blue wire on the igniter, which is the tach signal. Also I thought I would note that tunerstudio is displaying the RPM's, so ms3x is receiving data. https://www.miataturbo.net/attachmen...ine=1395233039 https://www.miataturbo.net/attachmen...ine=1327066127 |
hmmm after wiring the diode on both Idle Valve wires instead of just the +12v I get a loud hum from the TB area and no cranking...what did I do wrong here?
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humming noise is normal for the idle valve until you adjust the frequency. No idea why it would not crank though..
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TPS calibration set in tuner studio?
Also the frequency for the NB idle valve is 511Hz . |
Originally Posted by Jeffbucc
(Post 1121797)
hmmm after wiring the diode on both Idle Valve wires instead of just the +12v I get a loud hum from the TB area and no cranking...what did I do wrong here?
https://www.miataturbo.net/megasquir...hen-key-78404/ |
Yeah frequency was set to 511hz, but still no start or even coming close to cranking. I'm still receiving power to MS, but upon listening to the car more closely when attempting to crank, the fuel pump is now turning on upon cranking.
I'm going to go buy some more fuel and see if that has anything to do with it. I only put a gallon or so in so who knows. |
Also MAP is reading around 180+ degrees now...what the hell did I just do.
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Originally Posted by Jeffbucc
(Post 1121797)
hmmm after wiring the diode on both Idle Valve wires instead of just the +12v I get a loud hum from the TB area and no cranking...what did I do wrong here?
this is me just staring at the screen disapprovingly... |
Originally Posted by Braineack
(Post 1121847)
this is me just staring at the screen disapprovingly...
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well, the picture you posted of the diode is a correct way of wiring it.
what's the freq. of your idle valve set to in your msq? it needs to be much higher for an NB valve vs. the 93 of ~200Hz. I personally would have wired the tachout to 2I which sends it directly to the ignitor, then all you gotta do is connect teh y/b with w/b wire. |
Originally Posted by Braineack
(Post 1121851)
is a
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Also I set the frequency to 511.
That makes so much sense on the tach out wiring, jesus why didn't I see that... |
I do it inside the case. but same idea: banded end to 12v, non-banded end to the output/signal wire.
I would have done it inside your DIYBOB if anything. would have been much easier than hacking up wiring. |
Originally Posted by Jeffbucc
(Post 1121855)
Also I set the frequency to 511.
That makes so much sense on the tach out wiring, jesus why didn't I see that... |
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